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This started for me a few days before the event with
people ringing me up and
panicking about log books.
Friday had Denis Wright, secretary for scrutineering committee,
ringing me up
to ease up the pressure and left me with a definite way out for
those who have
attempted to obtain log books.
I was trying to be at Tong for 10.00 a.m. but due to my
reluctance to escape
from my bed I arrived at 10.45 a.m. Gareth Almond, clerk of
course, had already
worked out a course and with an ever growing band of helpers,
proceeded in groups
to mark out the 2.4-mile comp course.
The incompetence of the equipment officer (it's me) to check out
the staple gun
made the job of arrow fixing a little longer. It has been
repaired on site and it's fully operational. Now plans are afoot
to obtain more staple guns identical to the one and only.
We had 22 motors to do 8 runs each, the first 100yds of the
course saw PENNINE and NORC motors learning the lesson of easing
into the water troughs and powering out was better than powering
in and put-putting out!!
Everyone seemed to enjoy themselves.
Thanks go to all those who set out on Saturday with clean sticks
and arrows.
Also thanks to the people who brought in the muddy sticks and
took off all the arrows to make it easier for me. The staples
are out and the arrows are washed for another event.
My electric air pump has been used and abused by various people
over the last
year and will not be tolerated any more! If you want air for
your tyres BUY YOUR OWN PUMP!!
Sorry about the last paragraph but some people take all and give
nothing back
to the club, as opposed to the few who give time and effort and
take my grateful
thanks away!
Michael
Chaloner
President
Scrutineer
Equipment Officer
Assistant Editor
Tower of club trailer
Michael's never ending project
Life of my different motor started out from the moment I
returned from holiday
in
France
in the confines of a superbly coil sprung car to getting into my
leaf sprung Landrover and feeling every bump in the road.
A rolling chassis was located at a local scrapyard and there
began a two-year
crusade to get it built and on to the road. Part way into this
rebuild friends kept saying to me: "Oh you can't enter the club
events with that!" "Oh dear (or something similar) I'll carry on
building it then."
The trials and tribulations of a total rebuild or the ups and
downs of a never-ending project.
I will attempt to write in the order of:-
ENGINE, GEARBOX, PROP SHAFTS, AXLES, SUSPENSION, WHEELS AND
TYRES, COOLING SYSTEM, STEERING, BODY AND INTERIOR. ANY NOT
PREVIOUSLY MENTIONED.
ENGINE
I originally started out with a V8 from a Rover 3500 which later
in its life dislodged an air intake sleeve (carb), to do a dance
on most of the pistons and cylinder heads.
There's not a lot of room in a 10.5 to 1 engine. The next engine
came out of a, a,
a, Reliant Robin, three wheeler type. No joking! V8 plus auto
box in an odd legger
— three pin plug, blue in colour. The bores of this one
eventually came to light later in its life. Still a lover of V8
power, another engine was obtained, the present one.
This one is 9.35 to 1 out of a SDI Rover with, if I remember,
20-thou oversize pistons.
I had been cleaning the grooves out under the piston rings, and
yes, I unfortunately broke one. Tough, eh!
Retrieved good camshaft and suitable followers from the previous
engine and
we can rebuild. I fitted LUMENITION electronic ignition, and a
FACET fast road type pump sends 4-star leaded fuel to the SU
carbs. The carbs were always flooding, so I took the motor over
to G.R.V. Developments in Rochdale for an engine tune. He found
the problem in five minutes, no fuel return. "Go away and sort
it out". Two days later I was back again. 100 BHP at the wheels.
Oil and filter and changed regularly using semi-synthetic oil.
Look after your
engine it will last longer. The exhaust system was made and
fitted locally out of
stainless steel.
GEARBOX
This is a Borg Warner Type 66 automatic gearbox coupled up to an
Ashcroft
transfer box conversion.
I bought the gearbox and second-hand torque converter from lan
Ashcroft which
lasted about a year in service before a total stripdown was
needed together with a
NEW torque converter. When we were down at the ARC National at
Eastnor Deer
Park, we had gone into Ledbury to make a phone call home when 'Ie
crunch' occurred.
After a tow back by a lightweight to the camp site, an
exploratory examination
came into being. The drive end of the auto-box had sheared. A
journey back home
on the back of an RAC registered transporter was needed.
When I contacted lan Ashcroft about obtaining a replacement he
said an SDI
car drive end was needed. Wrong! After going to several scrap
yards and even two
auto specialists, the SDI end was too short and the wrong
profile.
I already had a BW 35 end which was the right profile but too
long. My boss
from work turned it down on his lathe in about two minutes. Six
miles back home
and 30 minutes later the motor was mobile again.
PROPSHAFTS
Having a different gear and transfer box than normal means that
the propshafts
have to be different. I struck really lucky here as the rear
length needed to be 41" between flanges, an S3 rear prop was the
same. Two and a half years of this in
operation led to serious vibrations over 40 mph. One way out of
this is to fit a genuine propshaft at £225.96 plus VAT or try
another second-hand one.
I wonder which way to go!!
What I did do, was to put another short sliding yoke assembly
on. On road test
the vibrations at 40 had disappeared but reappeared at about 70
mph.
The front prop shaft needed to be about 17" long. The yokes of a
rear Range
Rover prop shaft can go to greater angles (cut away more). The
one I had in stock
was taken to a place in
Bradford to be checked and altered and the balance checked.
I told them it was to fit a R.R. front axle, that means that the
yokes at the ends are out of phase because of the tilting
upwards of the diff.
They had put it in phase! Also on the front prop I had to fit a
non-genuine gaiter.
Genuine is best but don't take my word for it, go and waste your
money on a non-
genuine one. This led to mud, etc., entering past the perished
rubber, leading to the
splines seizing up.
AXLES
The front swivels were in a disgusting state of pitted rust and
occasional shiny
bits. Two courses of action were thought of. One was expensive
and buy new ones,
or the other was to take them to Vernon Moss, chrome and nickel
platers in Brighouse.
The first one I took was the good one. Mr. Moss said it was in a
sorry state. The
final outcome were two nickel plated swivels in a beautiful
condition. The differentials have a ratio of 3.9 to one.
SUSPENSION
The front springs are R.R. with the rear ones being
'90' rears. Front and rear
shock absorbers are standard. The rear ones are not originally
from the rebuild
because under extreme axle movement, one eye at one side and the
top of the rod
at the other side on separate occasions broke off. I have now
fitted axle straps to
hinder the total suspension travel.
All the bushes were new. The panhard rod is on its second set of
bushes. Four
bushes at the front of the front radius arms and the two bushes
at the front of the
rear arms have now been poly-brushed as the originals were
tired. Rear wheel steering on corners is not very good on the
heart!
WHEELS AND
TYRES
I currently run on eight spokes and trakkers. A word of warning
here — my tyres
are supposed to be tubeless on tubeless rims, but so far I have
had to put inner tubes in to keep the tyres inflated. For some
semi-serious off-road work, LWB rims and Goodyear X-tra grips
are used.
COOLING
SYSTEM
This is a radiator for a 110" V8 with hoses adapted to fit my
engine. Two (or
is it twin?) Kenlowe fans cool it down although in winter months
I keep the rad muff closed and keep an occasional eye on the
temperature gauge. Coupled up to a '90' heater system, MAGIC!.
Plans are afoot to vent the door glass from the heater.
STEERING
It does, thank goodness.
BODY AND
INTERIOR
From the front and including bulkhead, its '90' doors are Sll,
back body is a
genuine 100" and was in an unused condition, hard top sides are
'109' shortened
at the front and the roof is also '109' shortened at the rear. I
had two roll bar hoops made and fitted by Steve Dobbie, They are
all removable. Front seats are Volvo 3 Series and the rear ones
are Maestro.
I fitted a dim-dip resistor to facilitate the dipped headlamps
and found to my
annoyance that when I turned off the ignition, the engine was
still running and when
I turned off the headlamps shortly afterwards, the engine
stopped. I have since fitted a 25 amp diode into the system to
cure the problem.
I have one of those Unipate batteries from Express Factors in
Halifax that is
guaranteed for life. I have found that if you have a motor for a
long time, it pays in the long run to have such a battery.
THE
CHASSIS
The backbone of the whole vehicle. It is registered as 1972 —
nearly as old as
me — as a Range Rover. As some, or should it be all of the
outriggers are now not
required; I cut them off and ground away the remains with an
angle grinder. The
bulkhead outriggers were sourced from Hobson's at Louth and I
suspect that they
are from a prototype 100" chassis and the other outriggers for
the back body were made by myself.
The front of the chassis was cut by one inch or so to fix the
bumper on and the
rear end was shortened by about three feet. All the welding was
done by a professional welder using 3-phase
equipment.
Michael Chaloner, Club President
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